Question for Pro Boxer or The Mechanic
...or anyone else who knows about these things.
Recently tried BB chip, Y piece, K&N etc on my S but found it ran a bit too buzzy for my liking. Unsure if it was down to weak running I briefly tried a techlusion unit and then returned it to stock before getting to the dyno as it didn't feel right.
Getting to the point it appears (having re-read the manual) that I have committed a cardinal sin by disconnecting the motronic unit without disconnecting the negative battery lead when I installed the BB chip. To make things worse I have done this 3 times in all.
My question is have I buggered something up by doing this as although it is now stock again it still runs buzzier than before I started making any mods.
Acceleration and fuel consumption are unchanged and I have had a moditec check done that gives a 'no fault' read out so I assume I have got away with it?
It's just that the bike doesn't run as well as before that makes me wonder if one of the sensors isn't happy or the motronic is not 100% and giving a false read out?
The only other thing that occurred to me was that the 500 miles of possible weak running may have casued some damage to the exhaust valves as the tappet noise is definitely louder than before.
Any thoughts or ideas greatly appreciated as otherwise this is going to bug me on my France trip in 9 days time.
Cheers
Adam
...or anyone else who knows about these things.
Recently tried BB chip, Y piece, K&N etc on my S but found it ran a bit too buzzy for my liking. Unsure if it was down to weak running I briefly tried a techlusion unit and then returned it to stock before getting to the dyno as it didn't feel right.
Getting to the point it appears (having re-read the manual) that I have committed a cardinal sin by disconnecting the motronic unit without disconnecting the negative battery lead when I installed the BB chip. To make things worse I have done this 3 times in all.
My question is have I buggered something up by doing this as although it is now stock again it still runs buzzier than before I started making any mods.
Acceleration and fuel consumption are unchanged and I have had a moditec check done that gives a 'no fault' read out so I assume I have got away with it?
It's just that the bike doesn't run as well as before that makes me wonder if one of the sensors isn't happy or the motronic is not 100% and giving a false read out?
The only other thing that occurred to me was that the 500 miles of possible weak running may have casued some damage to the exhaust valves as the tappet noise is definitely louder than before.
Any thoughts or ideas greatly appreciated as otherwise this is going to bug me on my France trip in 9 days time.
Cheers
Adam